KAJIAN OPTIMALISASI JARINGAN DISTRIBUSI AIR BERSIH (Studi kasus : PDAM Delta Tirta Sidoarjo Unit IPA Krian)
Development of an area often gives either positive or negative effect. Creation of new district in some area requires the adequate infrastructure to support their activities, including infrastructure for water service. The needs for clean water can be done in several ways, such as using common pipin...
Saved in:
Main Authors: | , |
---|---|
格式: | Theses and Dissertations NonPeerReviewed |
出版: |
[Yogyakarta] : Universitas Gadjah Mada
2014
|
主題: | |
在線閱讀: | https://repository.ugm.ac.id/128506/ http://etd.ugm.ac.id/index.php?mod=penelitian_detail&sub=PenelitianDetail&act=view&typ=html&buku_id=68855 |
標簽: |
添加標簽
沒有標簽, 成為第一個標記此記錄!
|
總結: | Development of an area often gives either positive or negative effect.
Creation of new district in some area requires the adequate infrastructure to support
their activities, including infrastructure for water service. The needs for clean water
can be done in several ways, such as using common piping system that is managed
by the Regional Water Company (PDAM).
The research was conducted on PDAM Delta Tirta Sidoarjo of IPA
Units at Krian, by performing simulations with Waternet 2.2. Software. Network
Billing data from PDAM Delta Tirta Sidoarjo of IPA unit at Krian is used to
determine the existing data of amount of water consumption in 2012
(liters/person/sec), while the development is conducted by calculating the
population projection and water demand projections based on Master Plan for
Water Supply at Sidoarjo in 2011, then the results will be included in the node
needs of customers.
Simulation results from Waternet to existing network with fluctuated
flow shows that the performance of the network system is not optimal yet. There is
still laminar flow in 26 pipes and low pressure on the service node, that is 9.88
mH2O, such as at Sirapan, Kemangsen and Jagalan. Optimization of existing
networks is conducted by enlarging the small diameter pipe from sub node of
ô��ô���ô���ô���ô���ô���ô���ô��� ô���ô���ô��� ô���ô���ô���ô���ô���ô���ô���ô���ô��¶ô���ô��� ô���ô���ô���ô���ô���ô��� ô���ô���ô���ô���ô���ô���ô���ô���ô��� ô���ô��� ô���ô���ô���ô��� ô���ô���ô���ô���ô��� ô���ô���ô���ô��� ô���ô���ô���ô���ô���ô���ô���ô��� ô���ô���ô���ô��� ô���ô���ô���ô���ô���ô���ô���ô���ô���ô��� ô���ô���ô��� ô���ô���ô���ô���
tank. Water discharge of pump no.2 must be set, also the head following the new
tank. Optimization shows better result compared to the existing conditions due to
efficient work of the pump for 14 hours in average, while the existing condition of
the pump is working for 24 hours. Pressure left on the nodes after optimization is
better because of an increase in pressure at all nodes, i.e. 11.53 mH2O. |
---|